THATpreston
Brush your teeth.
- Joined
- Apr 30, 2006
- Messages
- 5,179
Thats haulin' for a streetable car.
It would be a perfect candidate and the course is in my backyard this year to boot. However, I don't have a job as of last Friday. Kinda hurts the play funds but I have time to play now.how come the S10 isn't on this Brandon? One would think Nat would do just fine...
Man..that sucks. Bad part?
Last years NX motor did not put a rod out but did burn a piston when they put the wrong tuneup in the ECM for the Texas mile. It was way over fueled and burned it up, operator error by the NX boys. It ran the Hotrod Tour fine the whole time, I believe it made a few passes in the 9's last year.
Larry Larson's a friend of mine and he won it last year and hopes to repeat this year. I truely believe his Chevy II will make a very low 7 second pass at over 200mph and just maybe a high 6. Unless someone puts a better number up Larry will run it just hard enough until he gets to the last track. At that point as long as the track will take it, it will be balls to the wall!
They could not change the tune up in the ECM. Not there fault.
Curtis Halverson supplied/built the motor and supplied the standalone controller and tuning. While I was not there I was told that they did have the ability to change the tunes but they had not learned what did what. Bottom line was they changed it on there own and burned up a perfectly good motor up. It ran well (9.9x 142.91 with a missed shift to boot) and for something that was just put together in time to make drag week from scratch.
Diesel Tech, You are spewing BS that is incorrect. No one at NX ever had the ability to tune anything on the old stand alone computer. The tune that was ran at drag week 08 was programmed by Curtis' guy Volker. The tune that was in the car at the texas mile was again programmed by Curtis' guy Volker. All that being said, i am not convinced the tune was the problem.
Curtis Halverson supplied/built the motor and supplied the standalone controller and tuning. While I was not there I was told that they did have the ability to change the tunes but they had not learned what did what. Bottom line was they changed it on there own and burned up a perfectly good motor up. It ran well (9.9x 142.91 with a missed shift to boot) and for something that was just put together in time to make drag week from scratch.
It ran better today. 9.8 at 142.9 Spining thru 2nd gear. I and no one else are trying to place blame on Curtis. So please dont get your panties in bunch. The new engine has parts from Curtis, yourself and others. If I made it sound like I was blaming Curtis I was not. I use Curtis's parts in my own engine also. I got involved because they (Mike and Tommy) wanted the abilty to tune the engine on their dyno. They could not do that before. The ECM need mailed back to switch tunes. I have no Idea what Greg said about it. But I know what Mike told me. He owns the car so I take him for his word.
This year was a simple, install the motor back in its place and put a different controller in place. They didn't have to start over at all as everything was in place and worked out. IMO to try and blame someone for that is BS especially after what they did with the motor and all. Then to not want to pay to fix it kind of tops it all off.
Nothing simple about a complete rewire and ECM change.
Rumor has it the '57 Chevy broke a motor so it's done.
Trashed a starter from what I heard.
Curtis Halverson supplied/built the motor and supplied the standalone controller and tuning. While I was not there I was told that they did have the ability to change the tunes but they had not learned what did what. Bottom line was they changed it on there own and burned up a perfectly good motor up. It ran well (9.9x 142.91 with a missed shift to boot) and for something that was just put together in time to make drag week from scratch.
Diesel Tech, You are spewing BS that is incorrect. No one at NX ever had the ability to tune anything on the old stand alone computer. The tune that was run at drag week 08 was programmed by Curtis' guy Volker. The tune that was in the car at the Texas mile was again programmed by Curtis' guy Volker. All that being said, i am not convinced the tune was the problem.
Johnboy
All I can say is what has been done in the past and it's true. The car ran last year and it never got dialed in as there was just no time. It finished the Power Tour just fine and got burned up after the tune was changed. If they had really wanted to work with the builder tearing his motor to pieces was not the way to go about it! Now they try to infer there was something wrong with the build! Seems to me when it came time to step up, they stepped out.
No one is inferring that someone was wrong with the build. At least not me, Tommy, or Mike. It burnt down the engine. They went a different direction with this one. I can remeber talking with Curtis about the engine being burnt down and how he was exicited to see it. To learn from it.
As far as changing the engine wiring and installing the new ECM after the entire car was already wired up is one hell of a lot simpler and when you've had over 6 months instead of 2 weeks, in my book that's a lot simpler.
The old ECM and harness where long gone before the engine was rewired. I never ever laid eyes on it. No way to learn from something you have never seen.
The car runs well and that was proven out last year, I just do not much care for what they pulled afterwards. Mike is a nice guy I just believe this time they did not step up and do the right thing.