Big Blue24
Comp Diesel Sponsor
- Joined
- Jan 5, 2008
- Messages
- 6,320
I finally pulled all the rockers and torqued my head bolts.
However, before I started, I checked valve lash after 60K miles of daily driving, hot rodding, and 20 or so 3900 rpm 1/4 mile passes. All of the exhaust clearances were between .019 and .020, all of the intake clearances were right at a snug .010. I was impressed that the valve lash was well within spec and dang near perfect considering the motor has 245K miles and it's been 60K since last valve lash job.
On to the headbolts, about half of the bolts moved/snugged up with just 90 ft lbs on the torque wrench. I then took all up to 100, then 110, then 120, then 126 ft lbs. Motor was still warm probably between 75 and 100*F.
I then replaced at valvetrain components in exact original positions and checked valve lash. All of the exhaust lash now came in at .015-.016 and all intake lash came in at .06.
The change in valve lash is proof to me that retorquing the stock head bolts does in fact provide more clamping force on the head gasket. On my well used motor, I feel confident that I compressed the gasket .04".
So Comp and ARP can claim that they tested stock bolts to yield and found no additional clamping load all they want, the truth is in the valve lash clearance changes.
Thoughts, comments, or criticisms?
However, before I started, I checked valve lash after 60K miles of daily driving, hot rodding, and 20 or so 3900 rpm 1/4 mile passes. All of the exhaust clearances were between .019 and .020, all of the intake clearances were right at a snug .010. I was impressed that the valve lash was well within spec and dang near perfect considering the motor has 245K miles and it's been 60K since last valve lash job.
On to the headbolts, about half of the bolts moved/snugged up with just 90 ft lbs on the torque wrench. I then took all up to 100, then 110, then 120, then 126 ft lbs. Motor was still warm probably between 75 and 100*F.
I then replaced at valvetrain components in exact original positions and checked valve lash. All of the exhaust lash now came in at .015-.016 and all intake lash came in at .06.
The change in valve lash is proof to me that retorquing the stock head bolts does in fact provide more clamping force on the head gasket. On my well used motor, I feel confident that I compressed the gasket .04".
So Comp and ARP can claim that they tested stock bolts to yield and found no additional clamping load all they want, the truth is in the valve lash clearance changes.
Thoughts, comments, or criticisms?