You can see here the cut outs for the O-ring, in addition to the added carnage from when I bolted up the valve body on last evaluation.
I also inspected for any new signs of any metal or spring and nothing was found.
I went ahead and performed the air check and no massive air leaks were noticed and 2C and 4C both held 30psi and you can hear 4 engage with pressure.
https://www.youtube.com/watch?v=J3HzXr9rkrg
Went ahead and replaced seals on billet pieces(have oem ones ready for a backup), torqued unit all around to 110in lbs and refilled.
Noticeably better and now its acting normal. Now I plan on seeing what the CVIs are soon, and then allowing the trans to do an adaptive relearn.