Kronic_187
Mekanical injection junky
- Joined
- Sep 27, 2009
- Messages
- 1,343
Well a month later after resetting my vavles and fixing the problem, i pulled my 5x.014's and had them pop tested ( all of them sticky, popping between 280 and 250bar) so i tossed in a set of the thin .020 washer under my stocker injectors and did a retorque and valve set.... 3 days later my #1 exhaust is wayy outta wack again, so this time i set my hot lash 2 .06 and .016 (i have a +.010 thick hg and rotated my engine by hand to make sure of clearance) trcuk ran fine for a few days.... then today i did a fairly long hill in 4th gear 2 about 1900rpm, coststant load @ about 10psi and 1900rpm... not really chugging it or over revving it, when i stopped it was thumping... sure enough #1 exhaust is slightly outta wack again. reset it to .016 again and seems to run fine.
Can anyone think of a reason why that nut would back itself off ? pushrod height does not change so i doubt it's a lobe or lifter, and spring height has not changed either. Seems like it works itself loose... this time when i set it, i torqued it to 25 ft/lbs and soaked the nut and adjuster in brake clean....
ideas ??
could it possibly be the early signs of popped hg ??? (sumhow////)
i have the pacbrake 60lbs springs in this head on the exhaust an intake sides.... perhaps this one has been pounded out and it's causing the problem ???
Can anyone think of a reason why that nut would back itself off ? pushrod height does not change so i doubt it's a lobe or lifter, and spring height has not changed either. Seems like it works itself loose... this time when i set it, i torqued it to 25 ft/lbs and soaked the nut and adjuster in brake clean....
ideas ??
could it possibly be the early signs of popped hg ??? (sumhow////)
i have the pacbrake 60lbs springs in this head on the exhaust an intake sides.... perhaps this one has been pounded out and it's causing the problem ???
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