I just had the head cut and put a new gasket on with the extreme-studs. The studs are a none stretch head stud and the paper says a 12 mm stud to 105 ft. lbs. of torque. I torqued in sequence from 60 to 80 then to 95 then 105 and checked all of them again.
Got it running today and drove it about 50 miles. Everything seemed good so I took the cold pipe out to set the 351 wastegate. Got it set at 30 lbs. hooked the cold pipe and took it for a drive. Ran it up to 40 lbs. of boost and pop, frickin head gasket let go out the front. Checks a few random studs and all were tight. It blew the first time out the side but the head took .015 cut to get it flat.
Any suggestions on what I could have done wrong? We will pull it tomorrow and lick it one more time. I just don't understand how it let go with a flat head, good studs and new gasket at that low of boost. I run more boost all the time on my 24 valve with stock head bolts and gasket with 329000 miles on it.
Got it running today and drove it about 50 miles. Everything seemed good so I took the cold pipe out to set the 351 wastegate. Got it set at 30 lbs. hooked the cold pipe and took it for a drive. Ran it up to 40 lbs. of boost and pop, frickin head gasket let go out the front. Checks a few random studs and all were tight. It blew the first time out the side but the head took .015 cut to get it flat.
Any suggestions on what I could have done wrong? We will pull it tomorrow and lick it one more time. I just don't understand how it let go with a flat head, good studs and new gasket at that low of boost. I run more boost all the time on my 24 valve with stock head bolts and gasket with 329000 miles on it.