Back Driveshaft shortened, front lengthened, got a tranny cooler.
Filed out the ford throttle cable hole square so the dodge snapped in place, even hooked to the ford pedal.
351 turbo coming from Lostinwalmart. I had to do some cross breeding with the dodge and ford tranny linkage, they work opposite directions, but I think I have it.
Original manifold turbo was tight to the HVAC, industrial manifold my 35 outlet is pointed at the block, now I'm going to cut and turn the outlet. 4" downpipe.
Put 60 miles on it, mostly good got a valve cover leak, overdrive intermittent, going to do some tuning on the shifter linkage on the trans, kind of vague, otherwise love it!
Reverse band anchor came apart yesterday morning, went to back up and it was really weak. So ended up pulling tranny yesterday, got most everything back together last night, just got driveshafts and fluids left. Then I guess I'll try it again.
Great you got it going always come up with some kind of trouble for a little bit.
I finally picked up EFI Live so I can do program my Allison better.Hopefully all problems are done with.