Big Swole
MegaInterceptor
- Joined
- Jun 28, 2007
- Messages
- 16,950
Well, Last Friday I went to the track to see what was up....Still have a power loss issue but that's beside the point right now..
After my 3rd pass, I noticed the water temp. climbing up pretty good...I knew something was up cause my truck never does that....Parked it and looked under the truck and had MAJOR blow by.....Took the oil cap off and samething...Ugh!!
Had it towed to Jeff's and spent the night there...Next morning I pulled the VC and injectors out....Bore Scoped it and THOUGHT it looked like I had 2 melted pistons....#1 & #3 looked wierd...
Just pulled the Head off Wed. and come to find out, ALL the pistons were fine and the HG was Perfect!!! (Still stock bolts BTW).....BUT, I blew out one of those little Freeze Plugs inside the head and that dumped a Chit load of Antifreeze into my motor!!! Thank God I had it towed!!!
What the best fix for this to not happen again??? It was on Cyl. #5 I think...Just above the Exhaust port!! Jeff thinks that since the metal is So thin there at the exhaust port that those are getting WAY hot and thats why it came loose..not from the pressure really ...My truck doesn't turn much above 3600-3700 rpms...
Jeff had and Idea about Tapping those openings and putting a threaded plug in there!! What do you think???
I heard that Tim Barber may have done this before but it wasn't cost affective....
I'd love to fix it soon ( least amount of money Poss)....So I can maybe make the Race in Sept. with NADM here in Reynolds GA...
Suggestions??
After my 3rd pass, I noticed the water temp. climbing up pretty good...I knew something was up cause my truck never does that....Parked it and looked under the truck and had MAJOR blow by.....Took the oil cap off and samething...Ugh!!
Had it towed to Jeff's and spent the night there...Next morning I pulled the VC and injectors out....Bore Scoped it and THOUGHT it looked like I had 2 melted pistons....#1 & #3 looked wierd...
Just pulled the Head off Wed. and come to find out, ALL the pistons were fine and the HG was Perfect!!! (Still stock bolts BTW).....BUT, I blew out one of those little Freeze Plugs inside the head and that dumped a Chit load of Antifreeze into my motor!!! Thank God I had it towed!!!
What the best fix for this to not happen again??? It was on Cyl. #5 I think...Just above the Exhaust port!! Jeff thinks that since the metal is So thin there at the exhaust port that those are getting WAY hot and thats why it came loose..not from the pressure really ...My truck doesn't turn much above 3600-3700 rpms...
Jeff had and Idea about Tapping those openings and putting a threaded plug in there!! What do you think???
I heard that Tim Barber may have done this before but it wasn't cost affective....
I'd love to fix it soon ( least amount of money Poss)....So I can maybe make the Race in Sept. with NADM here in Reynolds GA...
Suggestions??