Nice, about time you put a decent converter in there... Next weak point will definitely be the Input. Might not be a bad idea to drop the VB and swap out the Lock-up vent plate with one that has a smaller hole :Cheer:
BTW, did I miss how you are keeping your poor head gasket in one piece?? My stocker didn't much care for 60+ psi (my gauge only goes to 50 and it was way pegged out).
The head and gasket is stock with 245K miles. I overtorqued the head bolts to 150 ft lbs. I did not loosen or lube, just tightened them in 5 lb increments.
Did you have a boost leak last time you were at the track? I heard rumors of massive quantities of black smoke and 15 second ET's
Last time out, I didn't have lock-up. First pass was 13.75 and it wasn't loading the motor enough to get full boost so it was pretty smokey.
I then hot-lapped the truck about 15 minutes later and the tranny fluid was really warm. That resulted in a poor 15 second pass and only about 26 psi boost.
Third pass was a hot-lap as well about 25 minutes later and the tranny pan was still too hot to hold my hand on (I don't have a tranny temp gauge). That resulted in an even slower 15.8 second smokey pass and about 20 psi boost.
The single disk torque converter was built looser than stock and customized to help spool up a large single turbo with an oversized exhaust housing. When the fluid is warm and the lock-up clutch is toast, it just didn't provide enough load to make boost.
I have already checked the turbine wheel and wastegate on the He351 and it's just fine so I don't think I damaged a turbine wheel. It was just a lack load causing the low boost and therefore smokey passes.
I have not yet pressure tested the intake system so it is possible there is a boost leak, but upon visual inspection, all boots and connections are perfectly intact.