95' Junker Drag Truck

By the way, not to hi jack the thread but I know a lot of you were waiting for results on the DIY block o-ringing, I've had mine done (with the exact same tool and specs. And wire) for about a month and it's held up great. Reused stock bolts.
 
Those mods should make things interesting! Sorry for being impatient, it's just a very unique build and I like the DIY aspect of your truck.
 
By the way, not to hi jack the thread but I know a lot of you were waiting for results on the DIY block o-ringing, I've had mine done (with the exact same tool and specs. And wire) for about a month and it's held up great. Reused stock bolts.

You did that and then went back t stock bolts? Just doing an extreme budget build? And what are you at for timing, max boost, max rpm's, and miles since? And how many retorques have you done?
 
You did that and then went back t stock bolts? Just doing an extreme budget build? And what are you at for timing, max boost, max rpm's, and miles since? And how many retorques have you done?

Just had to get it back together on a shoe string. Rigt now I'm set at 19* max boost is around 55, max rpm is somewhere above 4k, miles are around 1200 and NO retorques.
 
No more budget? Also are you doing the mods one at a time to see performance difference

The low budget theme will continue.

- I picked up the used 215 pump for $600-ish, I'll be able to sell my maxed out 160hp pump for nearly the same amount so it's a "budget friendly upgrade".
- The roll cage was a necessity since this truck will easily surpass 11.50 ET in the 1/4 mile around $325 shipped to my door plus welding consumables and misc odds and ends for the seat, race belts, and padding.
- The fuel cell was picked up for around $100, too good of a deal to pass up, plus it will help with weight distribution for better traction.
- The ported head is a home-built DIY job so there is little cost other than carbide cutters and a few sandpaper rolls.

Unfortunately, the head porting, piston changes, honed cylinders and new ring package, and other not yet mentioned internal changes will happen at the same time so it will be difficult to quantify the power gains directly for each of these mods. The pump, and injectors will be changed after some baseline runs so at least the fueling and turbos will stay the same.... for a couple runs!!! :rockwoot:
 
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I think you will like the pump change. I just went from a 160 to a 180 and it pulls much better in the upper rpms!!! Can't wait to see your truck back at it.
 
I think you will like the pump change. I just went from a 160 to a 180 and it pulls much better in the upper rpms!!! Can't wait to see your truck back at it.

Even with the 160 maxed out?
So is a 215 maxed better than a 180 maxed with dv's? And I am assuming when you change stuff up on the 215, it no longer does the timing retard on top?
 
no you'll still get into the notches. but with the timing (im pretty sure) that Will is going to run it wont be a terribly huge factor. only way to keep out of the notches is to limit rack travel so it doesnt go into the notches :bang
 
Well if you change your mind and decide you don't want your 180, I'm accepting p pump donations

ha ha no way. Sticking with a ppump unless one day I buy a 4th gen as well. Planning on grabbing a set of 7x12's though. How have you liked them?


^^^Sorry to get off topic. ;-)
 
Even with the 160 maxed out?
So is a 215 maxed better than a 180 maxed with dv's? And I am assuming when you change stuff up on the 215, it no longer does the timing retard on top?

I went from a 160 with 191s, rack plug, 4ks and maxed on the truck to a 180 with .024s, 5ks, rack plug and maxed on the truck. I felt a noticeable gain in power with the same s468 charger
 
It's time to work on porting and polishing the 12 valve Cummins cylinder head. I had a cylinder head failure on another truck so i had to borrow the cylinder head from my Junker Drag Truck to get the other truck back on the road. This head was sourced used from Ebay for around $210 shipped to my door. It has a few minor cracks but actually looks to be in better shape than my original Junker Drag head. Since this head is new to me, I started out checking for flatness with a machinist's straightedge and found it to have 0.003" variance from one end to the other which is well within the factory service manual specification of 0.012" or so.

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Here's a picture of the stock exhaust port.
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Step one is the remove material from the short side of the port. There is a water jacket about 3/8" below the surface so you can't go too extreme.
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In this picture you can also see that the corner is worked over and the right side to help widen the port on the short side of the turn out of the bowl.
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Now reaching in there deeper to help blend the transition
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Now down near the valve guide there are some sharp corners from the factory machining: I smoothed these over but didn't really try to remove a lot of material, just round off the edges and clean up any large rough spots in the casting.
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I smoothed out the sharp edges but didn't really try to remove a lot of material, just round off the edges and clean up any large rough spots in the casting.
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I also removed material around the throat of the valve as seen in this picture. You can see the somewhat shiney 45* valve seat, then there is a 60* cut, then a large thick taper back to the casted port. It's good idea to leave most of the 60* cut below the valve seat in-tact and symmetrical with the valve seat edge above.
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A couple more pictures of the stock exhaust port to show the valve seat, 60* cut, and throat.

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After (1) 60 grit sand paper roll to clean up the rough carbide cuts:
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Next I reached in deep with the short carbide burr and started rounding the edge of the valve stem boss area.
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Now it's time to switch over to a long carbide burr than can reach in through the exhaust manifold port to finish the short side radius blending and clean up the casting flash in the port runner itself. I started by tracing a gasket's inside edge with a sharpie marker. Almost zero gain is picked up on a mild port and polish job by opening up the runner and gasket matching the port. This traced line just gave me a nice reference point to make sure the head port is equal to or slightly smaller than the manifold so I don't end up with a transition lip between the head and the manifold.
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From the exhaust port side, it's easy to touch up the area around the valve guide and finish blending. You'll also notice that more material was removed from the short side of the radius into the runner.

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A few rough spots in the the casting in the runner that need to be cleaned up
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All roughed-in, now it just needs some sandpaper roll work to blend my rough cuts and it will be finished.
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Will was rambling on about quad turbo's or something

took these spy photo's, AND! in one picture Ive captured 80% of the secret squirrel workings of the junker ;)

BEHOLD

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