Logged in to post exactly this. CompD I am proud...
Mild Tranny Carnage
I pulled the transmission last night (3 hours) I know I'm slow but to pull the tranny on my race truck there are a few extra steps: prop the truck up 18" so there is room to work under there, remove 90% of the twin turbo setup, remove the relocated transmission heat exchanger, remove both driveshaft loops, remove the homebuilt 5" exhaust system....
Anyway, my diagnosis was correct, the forward clutch pack was burned up. I created an experimental setup last time for this clutch pack and that's probably 90% of the reason for failure. The experimental clutch pack involved removing the plastic cushion spacer, installing two belleville springs instead of one, stock pressure plate, 4 clutches and 5 steels, flipped over pressure plate instead of stock .280" thick flat reaction plate, stock waved snap ring. The first thing I noticed is that the 4th clutch was just barely catching the splines on the ring gear and so it basically wasn't engaged, so right away I had a 3-clutch pack instead of 4. It also looks like the belleville springs flexed far enough to make contact with the planetary that mounts on the end of the intermediate shaft.
In this case a picture is worth a thousand words since I'm sure the above description is foggy at best:
I have same problem in my 47RH that I have rebuild in June/July 2012...
...hey, how did you get the tranny to shift at higher then 3000rpm?
Shaved down some of the governor weights? Mind sharing? How much weight, where, pix, etc...? I have hard time finding any brass/steel governor weights or any info on the subject...
:bang
I just finished reading this whole thing and wow I am impressed! definitely made a few notes for myself thanks for taking the time to do such a good write-up and thanks to everyone else who chimed in now i'm hooked i cant wait for the next update!
I liked the idea of pushing compressed air to help the turbo light faster, if it's feasible. wired up to a push button like how the ricers have for nos might not look so bad
Really nice job with the truck. mind me asking what you did with the overflow line from the injectors that ran back to stock filter housing? im building my fuel system now and unsure on my options
Just make a Tee into the return line.
No..its less pressure than the filter housing.
Really nice job with the truck. mind me asking what you did with the overflow line from the injectors that ran back to stock filter housing? im building my fuel system now and unsure on my options