Looks like I verified that the 03/04 trucks have a "wall" as some others have suggested.
With my setup I went 614 with DDP 50's. I went to a set of Flux 2.5's on new style bodies that were all blueprinted and whatnot..I got 624. I then installed the other set of nozzles I got to try (3.5+) and got 653. With the last change, my rail pressure was gonski with my modified stock CP3.
This week I installed a Dragonslayer pump and on the street, the midrange and topend were quite impressive, but normal driving wasn't much different. I did see a significant increase in the upper end RP.
Got on the dyno Friday night and put down 642. WTF, Mate?
Got the scanner on her and played with settings on the Smarty. Did back to back runs to verify RP (fine and holding 27k) and Calculated Load Percentage. This is where the problem lies...Max CL% was 68% as datalogged through the run. This would explain similar power with LESS smoke then before (better, consistent pressure). No rail pop or anything out of the ordinary, just no extra power.
Talked to Bob and he and Marco will be working on this issue when we host them for some tuning in early November.
In the meantime, I will try a TST on Sunday at our dyno day and see if the ECU fooling that it does corrects the issue. If so, we'll have something to shoot for with Marco. Hoping he can do electronically what the TST does physically.
Will post back here.
With my setup I went 614 with DDP 50's. I went to a set of Flux 2.5's on new style bodies that were all blueprinted and whatnot..I got 624. I then installed the other set of nozzles I got to try (3.5+) and got 653. With the last change, my rail pressure was gonski with my modified stock CP3.
This week I installed a Dragonslayer pump and on the street, the midrange and topend were quite impressive, but normal driving wasn't much different. I did see a significant increase in the upper end RP.
Got on the dyno Friday night and put down 642. WTF, Mate?
Got the scanner on her and played with settings on the Smarty. Did back to back runs to verify RP (fine and holding 27k) and Calculated Load Percentage. This is where the problem lies...Max CL% was 68% as datalogged through the run. This would explain similar power with LESS smoke then before (better, consistent pressure). No rail pop or anything out of the ordinary, just no extra power.
Talked to Bob and he and Marco will be working on this issue when we host them for some tuning in early November.
In the meantime, I will try a TST on Sunday at our dyno day and see if the ECU fooling that it does corrects the issue. If so, we'll have something to shoot for with Marco. Hoping he can do electronically what the TST does physically.
Will post back here.