Big Swole
MegaInterceptor
- Joined
- Jun 28, 2007
- Messages
- 16,950
Been chasing a loss in power lately as some of you know. Had some bad luck over the last couple of months with this thing...
Broken Input shaft right after my first trip to the track after the build...I may have injured it when I accidently locked my TC in 1gear on one of the passes....Anyway, it had been running awesome..best being my 11.47@117.88mph.....That calculates right around 790 on #2 only given a pretty accurate weight used....
After replacing the broken shaft, the next time at the track I had lost quiet a bit of power...three different times at the track only netted me right around the 12.00's at 111-112 mph....That is almost a loss of 100 HP.
Then I had the Htt turbo issue(s)...one, the pucks were getting stuck against the WG housing due to a bent/broke arm....two, I also had the thin plate on the WG that got warped and was blowing exhaust down on my S480....Sent it in a they did the temp. fix until the new fix gets online....
I did a complete Reflash of my ECM from a buddy that works for Dodge and nothing changed...
Well, started thinking I may have busted an injector or something....I've started getting more smoke and it's not cleaning up like it used to...Spool up is slower as well.....Went to the dyno day her in GA last Sat.....Did 691, 693, & 689......So, we confirmed that I still have an issue after the turbo was repaired......My Rail pressure is not the problem either cause I can hit 25K at WOT with my MP8 completely off...and 27.5K at WOT with MP8 on 100%
So today I pulled my injectors to send and get tested!!! But I did two things just to set my mind at ease..
Ran a bore scope down into the cylinders thru the injector hole...ALL cylinder walls, pistons and bowls look fine!!! It was a little difficult to see every little bit due to the fluid that falls in when the injector is pulled.......
Then, I did a complete compression test on all cylinders......I asked Jeff before I started what I should expect since my Piston's have been cut by a FULL .100......I think stock is around 470psi.....Jeff said he thought I'd be right around 375 psi.........Well, here's what I found:
#1 = 375 psi
#2 = 375 psi
#3 = 390 psi
#4 = 350 psi
#5 = 375 psi
#6 = 390 psi
Jeff said that everything was within spec.....I was a little worried about #4 being down a bit from the others..but Jeff didn't seem worried about it at all.....PLUS 25 psi down on one cylinders is NOT enough to lose 100 HP....
So, we totally ruled out ANY possible issues with my motor....Any Head gasket, Valve seat, Valve, piston, or ring issues would have shown up durring these test.......SO, it has to be a fuel issue....I'm hoping I just busted one injector body or something that won't cost too much....
My injectors will go out tmrw. morning......I'll keep everyone posted when we find the problem!!!
Any thoughts??? Please post up !!!!!!!!!!!!
David
Broken Input shaft right after my first trip to the track after the build...I may have injured it when I accidently locked my TC in 1gear on one of the passes....Anyway, it had been running awesome..best being my 11.47@117.88mph.....That calculates right around 790 on #2 only given a pretty accurate weight used....
After replacing the broken shaft, the next time at the track I had lost quiet a bit of power...three different times at the track only netted me right around the 12.00's at 111-112 mph....That is almost a loss of 100 HP.
Then I had the Htt turbo issue(s)...one, the pucks were getting stuck against the WG housing due to a bent/broke arm....two, I also had the thin plate on the WG that got warped and was blowing exhaust down on my S480....Sent it in a they did the temp. fix until the new fix gets online....
I did a complete Reflash of my ECM from a buddy that works for Dodge and nothing changed...
Well, started thinking I may have busted an injector or something....I've started getting more smoke and it's not cleaning up like it used to...Spool up is slower as well.....Went to the dyno day her in GA last Sat.....Did 691, 693, & 689......So, we confirmed that I still have an issue after the turbo was repaired......My Rail pressure is not the problem either cause I can hit 25K at WOT with my MP8 completely off...and 27.5K at WOT with MP8 on 100%
So today I pulled my injectors to send and get tested!!! But I did two things just to set my mind at ease..
Ran a bore scope down into the cylinders thru the injector hole...ALL cylinder walls, pistons and bowls look fine!!! It was a little difficult to see every little bit due to the fluid that falls in when the injector is pulled.......
Then, I did a complete compression test on all cylinders......I asked Jeff before I started what I should expect since my Piston's have been cut by a FULL .100......I think stock is around 470psi.....Jeff said he thought I'd be right around 375 psi.........Well, here's what I found:
#1 = 375 psi
#2 = 375 psi
#3 = 390 psi
#4 = 350 psi
#5 = 375 psi
#6 = 390 psi
Jeff said that everything was within spec.....I was a little worried about #4 being down a bit from the others..but Jeff didn't seem worried about it at all.....PLUS 25 psi down on one cylinders is NOT enough to lose 100 HP....
So, we totally ruled out ANY possible issues with my motor....Any Head gasket, Valve seat, Valve, piston, or ring issues would have shown up durring these test.......SO, it has to be a fuel issue....I'm hoping I just busted one injector body or something that won't cost too much....
My injectors will go out tmrw. morning......I'll keep everyone posted when we find the problem!!!
Any thoughts??? Please post up !!!!!!!!!!!!
David