I took the Junker to Las Vegas Motor Speedway last Friday night for the street legal midnight mayhem drags. I went in true street legal form and was running some half worn-out Wrangler MTR 285/75/16's at 35 psi with Kevlar reinforced sidewalls. They are heavy and stiff but seem to get a little more traction than the old 245 Michelins.
The truck has been taking longer and longer to spool up the large atmosphere and the problem finally showed up, it was a blown inter-stage boot right at the HT4B compressor outlet 45* silicone bend. The tear was on the underside and so I missed it during my troubleshooting sessions.
I lined up against a stock appearing 2011 Camaro SS, he actually had a 100 shot of nitrous on his otherwise 2 week old Camaro. It was a close race but he got me by a few feet at the line with a 0.056 second margin of victory.
Anyway, my truck ran slower and slower as the night progressed. Peak boost pressure also got lower and lower but I wasn't able to find the bad boot till I got home. I actually had thought that possibly the top turbo's turbine wheel was slowly eroding away.
On the 13.23 @ 114.3 run, the truck was making 65 psi boost.
On the 13.99 @ 112.6 run, the truck was making around 60 psi boost.
On the 13.92 @ 107.9 run, the truck was making 45 psi max in overdrive.
Even though my truck was running pretty slow, it was still fun doing big smoky burnouts with those Wrangler MTR's.
You can see the short radius 3.5" steel 45* I used to line the inside of the 45* silicone elbow, it's possible that the sharp edge of the 3.5" steel elbow contributed to the failure. All that I know is the truck had been much slower to spool the past few test rides and I'm glad the problem surfaced.
And here's the replacement part I made by welding a 45* bend to the 90* bend.